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I have obtained a prototype NetGain TransWarP-7 motor that was designed especially for hybrid conversions.  The motor generates about 40 HP and 75 ft-lbs of torque with the 72V and 450 amps the controller can provide.  This motor has a 1 1/8" input shaft giving about 92% more strength than the first ADC motor I tried, the shaft on that first motor twisted on me.  The ADC motor was on for 700 miles but as I was trying to isolate a slight vibration I found the shaft twisted and thus removed it.  See problems section if interested. 

 

To the right is a diagram of how the motor is installed.  I had two shorter drive shafts made up from one I picked up at a salvage yard.  This allows me to preserve the original driveshaft so I can reverse the process if necessary. 

Something I had to do once when the first motor shaft twisted.

Here is a picture of the new NetGain motor.  It comes with a slip yoke on a 1.370" 32 tooth shaft.  This is supposed to be the same spline cut as on a GM HD Turbo 400 transmissions.
Here is a shot of the motor attached to the front mounting bracket.  You can also see the short front driveshaft. 

The bracket slides over the torsion bar frame member.  The nuts welded on top allow for vertical alignment.  With 72V and a 450 amp controller the motor should produce about 40 HP, giving a 14% improvement in peak HP and a 22% boost in torque.   BUT since electric motors produce their maximum torque at 0 RPM, when gas motors are at their worst, it should give a noticeable boost in performance. 

Each of the 6 mounting bolts has a neoprene isolator washer used to isolate bridges in earthquake areas.  I am using this to help dampen vibration from the drive shaft. This is in addition to the rubber mounts on the torsion frame member.

The shop work on the front and rear motor mounts ran about $250.

This is a shot of the front of the electric motor when mounted in the truck.  You can also see the 0/0 power wires to carry the electric current from the controller to the motor.

I see this current frequently spike past 500 amps. 

 

Here is a shot of the front, shorter driveshaft to connect the electric motor to the transmission.  The U joints allow for a slight off-set but we did our best to line things up. 

I tried an offset to see if I can install a larger motor and unfortunately I had a vibration between 30 and 40 mph.  So I put the motor back into alignment.

 

 

 

 

This is a shot of the rear motor mount.  I adapted the bracket made for the ADC motor to this TransWarP motor.  While not ideal it does appear solid.  I used a combination of a Jeep transmission mount and some large neoprene washers.

The motor has a double wide bushing and a fitting for greasing. 

I think ideally I would have mounted to a plate welded to the top of the rear frame mount but I have run out of money and patience.

 
This is a shot with the custom rear driveshaft connected to the electric motor.

You can see my attempt to get everything in alignment with a laser tool.  The plumb bob is hanging from the end of the transmission yoke. 

Several have asked if the extra drag or friction will cause a drop in MPG.  Theoretically it should.  I have two test hills that I have been using to test this on a lightly traveled end of I-26.  It seems like MPG dropped by 1% on the trip up the hills with the instant MPG based on 8 averaged runs.  On the coast down I have also seen nearly a 1% decline in the speed in neutral.  So the drag does not seem to be very significant.

I crest the hill at 55MPH and depending upon direction coast to 70 or 75 on the downhill side

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